My quadcopter becomes unresponsive when I disconnect the Naze32 from my compter

Help! This is my first quadcopter build and I am having an issue where I unplug the usb cable from my Naze32 rev6 (I am using cleanflight) and when I try to do anything on my transmitter, nothing happens. There is just a solid blue light. I have been trying to get this thing to work for three days now, but no luck. Any help would be much appreciated
 
Do the motors spin up in motor test tab? Have you correctly calibrated gyro and mag? If so, it sounds like it's just not arming. What stick movements are you doing to try and arm it?
 
The motors are calibrated and spin in unison. I have the arm switch connected to the aux1 on my radio. The gyro and accelerameter are calibrated aswell. I can arm and control ny quad while it is connected to my computer, but when I unplug it i can not do anything.
 
Just curious. Even though you've got a switch set up to arm, move your throttle stick to the bottom right corner and see if that works
 
It does not work using the control stick to arm. I am powering my naze with a 3s lipo
So 5vts from bec or pdb? And your rx is powered on? jacksons after your power. When you power by usb it works. without usb hooked up it doesnt. Thats were you should look. What is the usb doing to the naze that your battery power alone is not doing?
 
Help! This is my first quadcopter build and I am having an issue where I unplug the usb cable from my Naze32 rev6 (I am using cleanflight) and when I try to do anything on my transmitter, nothing happens. There is just a solid blue light. I have been trying to get this thing to work for three days now, but no luck. Any help would be much appreciated
Wait so a blue light on naze or on rx?
 
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