Configuring my FCB

ram1000

Well-Known Member
I am unable to get my radio to indicate any communication to the FCB ( naze 32) while on Baseflight. moving the throttle forward and back gets no movement of the colored bar at the throttle. The problem may be that I have the RX cables out of order on the FCB but I think they are right. I need something to check the sequence at the FCB. Is the throttle on the far left or right? BY the way I had a successful bind after a couple tries but I have reconfigured the Radio (DX6) settings since then and can't get a new bind yet.

Also I have a motor that is acting funny. Sometimes it clicks and jerks as I bring the rpm up using my mouse in Baseflight. Just one motor(motor #1) does this and it ceases this event after a number of throttle runs, again using the mouse in Baseflight as my radio doesn't seem to want to talk to the FCB yet. All the motors all seem to start at about 1073rpms as indicated in baseflight. I haven't switched it with the opposite motor to see if it does it on the other ESC but will attempt that tomorrow.
THank you...
 
can this receiver be bind' without being connected to the FCB if I have power to the receiver, or is there additional data being transferred through the FCB as well at the time of binding?
Also is anyone familiar with the Naze 32 with pressure sensor? I am only getting the blue light on when I plug the bat in???
 
Well no replies but I am moving toward a finished flying DJI 330. to answer my some of my own questions:
I tried many times to bind to the Naze32 board with my Spectrum black receiver, but always unsuccessfully. So I bought a PPM orange receiver and it bound easily. The problem seems to be that in Baseflight there is a setting for the sbus or other type receivers and I guess it would not connect while the sbus was checked. Since I replaced the receiver with what I think is an sbus it worked without problems. This also cured my lights on the FCB since going to the sbus receiver all the lights respond accordingly.

My motor is still acting strange in that until it achieves 1500 or so rpms it just jumps around. This appears to be the ESC but I don't know if it is bad or not. I switched motors and the first motor works fine on another esc while the one I switched into the old place is not doing the same thing. At any rate the motor does alright after it warms up and achieves rpms above slight idle speed. The quad seems to behave at hover speed without jumping around as I would expect it should if the ESC was bad???

Now for more questions:
1.Do I need to buy another ESC?;
2. I have a naze32 board with pressure sensor- how do I get my DX6 to tell it to function off switch "H".
thanks???
 
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