Good evening,
I'm fairly new to the whole drone building experience, as I have had a 3D printer for a while now I came across printing Peons 230 quadcopter frame from thingiverse.
I've brought all the required parts to what I believe is correct, I'm also using clean flight to program the board. As you will see from the parts list attached below, they are a majority of my parts.
The issue lies upon getting a response between the controller and the drone. I have successfully binded the drone and remote and set the remote up for PPM - iBus it's just when I connect into clean flight and go into the receiver tab and try to move the throttle I receive no response what so ever, all of the boards are connected to power and the remote too.
Any advice would be extremely helpful, I have already blown an FP3 board today after getting a response and pluggin the battery into the drone and I don't want that to happen again.
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Parts:
- Flysky FS-i6X 10CH Radio Transmitter + Flysky ia6B RC Receiver (2.4GHz, AFHDS 2A, RC Transmitter)
- Matek 6S PDB with XT60
- Crazepony-UK F3 Flight Controller Acro Cleanflight 6DOF
- Crazepony-UK 4pcs EMAX RS2205 2300KV Brushless Motor 2CW 2CCW
- HAKRC 30A 32Bit BLHeli_32 DShot1200 ESC 2-4S
- 14.8V 1500mAh 65C