High pitch squeal from motors... FIX.

Long Range RC

Well-Known Member
Hello Guys, If you remember how I told you in an earlier post that the one Hornet I had the Tarot 2 gimbal on kept having a high pitch squeal followed by a uncontrollable turn? I think I figured it out. I noticed that the speed controllers I have had a setting for the timing of the motors. If you are running a motor with more than 6 poles it needed to be at 16 Hz but the default setting is at 8 Hz. I changed the settings and built a new hornet with a new frame and it flies great. I also noticed that once I switched the Hz that my gains dropped from 179 to 116.

Something to keep in mind on any new builds you might be putting together.
 
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