I've built a 250 drone, everything seems to be working. I've done a 24" hover, moved around at very low speeds, things seemed to be working, but then the coptor started diving to the front left. I'd be in a hover, and bang, it'd on the ground. The last time, it broke the prop, so I replaced it. With the prop replaced, yes, it's the right direction, I arm it, the props start spinning, and as soon as I try to give it throttle, it flips over on motor 3. Holding it in my gloved hand, I can throttle it up and the motor obviously cuts out under load. Is it possible to have a motor 'go bad' like that? I checked all the ESCs, the solder connections and wiring.
I'm stumped... short of replacing the motor, I'm not sure what to do.
I'm stumped... short of replacing the motor, I'm not sure what to do.