Shuff
Member
Hi Folks,
Just in process of building and testing my quad, my components are
250 fibreglass frame, multistar 2209-980 v2 motors with Gemfan Tri 5030x3 props.
Esc,s are multistar 12A race spec 32bit opto with Naze32 rev6 fc. Redcom cm703 receiver and XT60 PDB, Lipo 3S 11.1V 1500 battery. Total weight is 580 Grams.
I have followed the Naze32 setup as per Painless360 on youtube and am using cppm. The esc are calibrated I am using the Spectrum DX6I tx unit. The problem I have is the quad fails to take off.
The motors spinn up ok to the max 2000, when tested on a wooden floor the quad just creeps around the floor and won't go airborne.
What can be the problem ? Is it to heavy or are the props lacking in pitch any help would be much appreciated.
Just in process of building and testing my quad, my components are
250 fibreglass frame, multistar 2209-980 v2 motors with Gemfan Tri 5030x3 props.
Esc,s are multistar 12A race spec 32bit opto with Naze32 rev6 fc. Redcom cm703 receiver and XT60 PDB, Lipo 3S 11.1V 1500 battery. Total weight is 580 Grams.
I have followed the Naze32 setup as per Painless360 on youtube and am using cppm. The esc are calibrated I am using the Spectrum DX6I tx unit. The problem I have is the quad fails to take off.
The motors spinn up ok to the max 2000, when tested on a wooden floor the quad just creeps around the floor and won't go airborne.
What can be the problem ? Is it to heavy or are the props lacking in pitch any help would be much appreciated.