I've got a Hubsan x502s. I crashed is a couple weeks ago and killed one of the motors. Other than one prop not spinning, the copter was fine.
I replaced the motor and now it never gets past "calibrate compass 1" no matter when I try. I've rechecked my soldering job, made sure the connectors are seated well and re-bound the copter to the controller.
The copter makes a high pitched sound starting about 3 seconds after you connect the battery, which it only ever did before when it was not bound to the controller.
Any ideas what can cause this or how to fix it?
Thanks,
Chris
I replaced the motor and now it never gets past "calibrate compass 1" no matter when I try. I've rechecked my soldering job, made sure the connectors are seated well and re-bound the copter to the controller.
The copter makes a high pitched sound starting about 3 seconds after you connect the battery, which it only ever did before when it was not bound to the controller.
Any ideas what can cause this or how to fix it?
Thanks,
Chris