Xavier Hamilton
New Member
Just recently finished up building a Lumenier Qav-R FPV Quad. I used a PDB with an integrated OSD and a Dodo flight controller hooked up to 20A Dys ESC's and 2300kv Dys motors. This actually my first scratch quadcopter build. While I was testing the motors in clean flight motor 4 would not spin. Motors 1, 2 and 3 would spin just fine. I swapped the signal wire for motors 3 and 4 and motor 4 wou.00ld then spin just fine and motor 3 would no longer spin. Not sure what else to do at this point. Not sure if this is something software related or what, but something with the signal coming from channel 4 on the dodo must not be working properly. Any help or advice is very much appreciated. Thanks in advance!