Hi everyone, I'm a newbie and have had a few crashes with my Novice and up to this point no issues with repairs. However recently I replaced two motors and thought I would go onto beta flight to tamper with settings as I unknowingly had soldered the wires in the wrong order making motors spin incorrectly. After having resoldered two of the wires in the correct order everything seemed ok in Beta flight (motors spin to full capacity, switches AUX1 arm the quad on screen) but drone will not arm via the transmitter and unplugged from the pc. Not sure if I have touched a specific setting or could something have cooked or have been damaged on its last crash? Any Ideas guys? Much appreciated if someone could point me in the right direction