Hey Guys. Newbie to drones checking in. I recently purchased a walkera rodeo 110 rtf for my first drone. I noticed that it has a slight backwards throttle drift. I hooked it up to clean flight and noticed the accelerometers weren't calibrated correctly so I reset the calibration, but I am still getting the same problem. I have to push throttle slightly forward to get drone to hover correctly.
I was wondering if anyone could give me a couple tips on what I can do/check to fix this issue?
I was wondering if anyone could give me a couple tips on what I can do/check to fix this issue?