Naze32 issue

Enis Bukalo

New Member
Hello. So i am completely new to this hobby. I currently own a couple of HPI and Traxxas trucks but never a multi rotor. I set up my quadcopter with the Naze32 and I bought a flysky T6 transmitter that comes with its own receiver. I plugged it all in and hooked it all up and connected it to Cleanflight. The receiver is getting signals based off of cleanflight, but when i unplug it from the computer, the motors dont react at all. Also, when i manually test the motors, only motors 1 and 2 spin, 3 and 4 will not. Currently connected to a 2S lipo just for testing. Any help would be great thanks.
 
Is it setup as a quad in the settings in cleanflight?

Screen%20Shot%202015-02-07%20at%209.12.23%20pm.png


Also, do all motors spin while testing the motors in cleanflight?

Motors-Screen.jpg


 
No only motors 1 and 2 spin. I take out the motors plugged into 3 and 4, place them into 1 and 2, they spin also but 3 and 4 still don't spin. and yes it is setup as quadX
 
Do they all spin while testing the motors in cleanflight?

Sounds like the motors are ok, but need to make sure the escs are ok before finding the culprit.
 
I switched the motors from 3 & 4 to 1 & 2, (escs are soldered to motors) and they spun up. but just 1 & 2. all 4 spin from cleanflight, but only if they are plugged into 1 or 2, 3 and 4 don't respond.
 
Sounds like it could be a bad board. Is it a new one?

I don't think calibration is the issue, but did you calibrate the escs?

You could save your settings, and try flashing the board.
 
Last edited:
Oh poop thats what i figured, it was the board from HobbyKing, funfly version i guess. I just ordered the whole thing with GPS and BARO, hopefully it works lol thanks.
 
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