Good Day,
today i finished the building process of my new quadcopter.
Naze32 Rev6 Full
S550 Frame
30A SimonK Esc
100KV Motors
1045 Props
So the building part is done, all is neat and like i want.
I started the calibration and the initial setup.
Flashing Naze etc.
I use a Turnigy 9xr Pro with a sky-fry setup.
ESC calibrated like it used to be, also heard the sounds etc.
Now, please check screen attached here. I have a very strange behaviour.
I wanted to make a first test, props off of course, with the remote and the motors do not act like they should be.
If i move the slider in Cleanflight, they are all equal and working at the exact same rate etc., like it should be. (and they stay like this)
With the remote, they seem to do what they want even if i throttle up just a little bit, motor 2, goes higher and higher while motor 1 not even spinning.
If i throttle full, from zero, not all motors are at highest point.
So, throttle up over the FC with Cleanflight, all looks good, throttle up over the remote, chaos.
As i am new to this i am a little lost where to start the trouble shooting.
I checked the remote settings, all seems to be fine for me, as all is within the range.
Calibrated ESC again.
It is a new model.
The Range are good, from around 990 to 1945.
This is for all sticks, and all switches.
With an older, test FPV, it was working fine like this.
Even with the same FC is used.
Do you have any tips what i can do next?
Do you need more information?
Thanks in advance.
Regards
TheCrey
today i finished the building process of my new quadcopter.
Naze32 Rev6 Full
S550 Frame
30A SimonK Esc
100KV Motors
1045 Props
So the building part is done, all is neat and like i want.
I started the calibration and the initial setup.
Flashing Naze etc.
I use a Turnigy 9xr Pro with a sky-fry setup.
ESC calibrated like it used to be, also heard the sounds etc.
Now, please check screen attached here. I have a very strange behaviour.
I wanted to make a first test, props off of course, with the remote and the motors do not act like they should be.
If i move the slider in Cleanflight, they are all equal and working at the exact same rate etc., like it should be. (and they stay like this)
With the remote, they seem to do what they want even if i throttle up just a little bit, motor 2, goes higher and higher while motor 1 not even spinning.
If i throttle full, from zero, not all motors are at highest point.
So, throttle up over the FC with Cleanflight, all looks good, throttle up over the remote, chaos.
As i am new to this i am a little lost where to start the trouble shooting.
I checked the remote settings, all seems to be fine for me, as all is within the range.
Calibrated ESC again.
It is a new model.
The Range are good, from around 990 to 1945.
This is for all sticks, and all switches.
With an older, test FPV, it was working fine like this.
Even with the same FC is used.
Do you have any tips what i can do next?
Do you need more information?
Thanks in advance.
Regards
TheCrey