I have ar8000 rx and dx8 tx with a cc3d fc...... I'll have try next week as I have done my ankle in and I'm almost out of props lol..... and if everything is still on what does that mean ..software glitch ?....... and if it off hardware issue ?
What I was saying it that after about 5 mins the red quad would stop all together and drop from the sky ..... the battery still had life in it as I'd then use it on the green quad ..... I just wanted some ideas as to y the quad was dropping out of the sky ..... it's not a battery issue ..... and...
Well I've set up both quads exactly the same way but the red quad dropped from the sky and the green 1 didnt..... someone said look at the deadband setting so I'll try that at somepoint..... and I had only been in flight for about 5 mins if that with a fully charged battery .... I get about 14...
So took the quads out for a proper fly ...had the red 1 in the air for about 5 mins then it just dropped like the power had been cut ... any ideas .....the other day it did the same ...... could it b a glitch with the program set up at the time I did the auto tune ?
Then the green 1 went up ...
So I tried droning on both quads and there flying .... hovering ok ... but like to drift a lill ..... and seem a lill slow when auto leveling but there flying lol ..... the drift I can sort out with trims that's no problem but what do I need to adjust for increasing the leveling out speed
I have a naze 32 board but got it as a backup .... if I can't get these quads to fly it going to do my head in ...it's been a month already ..... dronin is the next test so fingers crossed
So the green zmr is flying and the same oscillations r happening that the red zmr has .... I have looked at a couple vids for pids and want to get confirmation on this .
P is to stop oscillations or cause them depending on what the setting .
I is to level the quad quicker or slower depending...
I'll have a mess around with it tonight after work but I'll try and get the other quad flying b 4 I mess with that..... at least if I can get the second quad in the air I'll b happy but we r making progress finally
Ok so took the red quad out for a test flight ......since I changed my quad type from zmr250 to generic it is now flying yay ....but .
The quad is not smooth in flight ...... very jittery ........ I had it in a hover about 3 ft off the floor and noticed it wobbling quite a lot ...not alot of...
Ok so I have tried changing from zmr to generic and it seems alot more stable .... couldn't fly it as it's raining here right now but held it in my hand ...... doesn't seem like it wants to flip but if I give a little bit of throttle it will stay at that throttle position until i move the quad...