Hi Sean , make sure the leads that run from motors to the kk board are right , some one else on here was having same problem ,so i did test on my quad i swapped 2 motor wires so i had m1 on m2 ,m2 on m3 etc and she flips , due to the board seeing the movement of the quad and telling the motor to speed up to balance quad but that signal was going to the wrong motor so it tips and fcb put more input in till its over this takes 1000 of a second faster than you can see , so check m1 to pins of m1 etc,the way i do it is pull all off but leave on motor 1 then power up see if motor 1 spins if yes move on to motor 2 unplug battery each time you plug a motor in then test ,then move on to next one
one last thing to check is the forward arrow on kk is facing forward